• conciselyverbose@kbin.social
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    11 months ago

    The US National Transportation Safety Board (NTSB), which is leading an investigation into the incident, said pilots had reported pressurisation warning lights on three previous flights made by the specific Alaska Airlines Max 9 involved in the incident.

    As bad as it is if a manufacturing issue caused a piece to fall off an airplane, there’s a huge amount of negligence in an airline continuing to fly an airplane that has triggered pressure warnings multiple times without investigating and resolving the issue.

    • n2burns@lemmy.ca
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      11 months ago

      And the next paragraph:

      The jet had been prevented from making long-haul flights over water so that the plane “could return very quickly to an airport” in the event the warnings happened again, NTSB chief Jennifer Homendy said.

      Which makes it sound like they couldn’t find the source of that warning but weren’t willing to completely write it off.

      Nevermind:

      “An additional maintenance look” was requested but “not completed” before the incident, Ms Homendy said.

      • Darorad@lemmy.world
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        11 months ago

        I mean I’d much prefer they didn’t fly a plane that was repeatedly saying there’s a serious issue with it.

        • trafficnab@lemmy.ca
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          11 months ago

          I’ll wait to pass judgement because, not being an expert, I have no idea what the standard procedure is for that warning appearing in 3 out of however many (hundreds of?) flights this plane engaged in over that period of time. With hindsight of course we can say “duh don’t fly the plane with the door about to blow off if it says it has pressurization issues” but maybe this is not actually a particularly serious warning in different circumstances.

          • methodicalaspect@midwest.social
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            11 months ago

            If I’m not mistaken, the Alaska Airlines accident aircraft completed 99 flights, as it went into service only a couple months ago.

            Not an expert myself but I binge air crash investigation shows like nobody’s business, and this seems to speak to QC and maintenance workload/culture issues.

      • highenergyphysics@lemmy.world
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        11 months ago

        Surely this bodes well for their acquisition of Hawaiian, which famously operates long trans-Pacific routes across thousands of miles of open water!

    • GombeenSysadmin
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      11 months ago

      Ex-aircraft mechanic here. Nothing will have been done in this situation without paperwork backing the decision. There are often small niggles that could ground an aircraft, but there are manuals that can be consulted to see how many more flights can be taken before it must be grounded for rectification - the MEL (minimum equipment list) and CDL (configuration deviation list). So the airline will not have made the ultimate decision to keep flying, Boeing will.

      The fact that this has now been found in two different airlines means that it’s a design flaw again, either the locking mechanism on the bolts is insufficient, or the reinstallation instructions in the maintenance manual is incorrect (the Alaska airlines aircraft door plug was recently removed to carry out maintenance on another part)

      • ursakhiin@beehaw.org
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        11 months ago

        As an airline customer, I would much rather have the airline tell me the plane was grounded due to parts being ready to fall off than the 3 hours I had to wait one time because of a busted tray table.

        • GombeenSysadmin
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          11 months ago

          If it’s not in the MEL or CDL then you can’t fly without it. They’re basically a book of approvals for how long you can get away with stuff.

          Btw If the tray table can’t be stowed, you can’t take off with anyone in that row because of the danger in an emergency landing.

    • JillyB@beehaw.org
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      11 months ago

      Agreed. This is a multi-layered fuckup. The manufacturer probably didn’t tighten things down all the way, their QA didn’t catch the critical defect, the plane inspectors didn’t catch it during inspection, the airline didn’t ground it after a pressurization warning, the pilot flew a plane with a known issue. There are several cultures of complacency at play. Hopefully the FAA can scare everyone into flying right.

      • conciselyverbose@kbin.social
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        11 months ago

        The reason I added the “if” is because I didn’t see any information about age and don’t know the specifics of the engineering/specs. Bolts needing the be checked annually and tightened every 5 on average could be perfectly reasonable with how much stress is on airplanes. There’s a reason frequent inspection is enforced more heavily on airplanes, and it’s not just because failures mean potentially falling out of the sky.

        But yeah, it’s entirely possible they fucked up, but it’s for sure United Alaska did.

  • Howdy@lemmy.zip
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    11 months ago

    MAX must stand for “MAX Profits” because they sure cut lots of corners on that aircraft.

      • Bytemeister@lemmy.world
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        11 months ago

        Probably more than you think. This strikes me as an understaffing issue in the factory. Loose bolts happen when the person who is supposed to verify the work has been done correctly, is busy doing work elsewhere on the plane. Understaffing causes people to pitch-in to make deadlines, or to ease the burden on their co-workers. Seems trivial at first, but with airplanes, this behavior gets people killed.

  • WetBeardHairs@lemmy.ml
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    11 months ago

    After looking at that diagram I have to ask - why in the everliving fuck would a pressure bearing panel like that be hung by bolts and not inserted into the cabin and held in place by the ribs of the fuselage? I mean seriously?

    • EeeDawg101@lemm.ee
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      11 months ago

      I don’t get why they don’t just make it a bit bigger on the inside so that when pressurized, the pressure itself seals it. Seems like a fail safe solution instead of this shadiness.

      • MigratingApe@lemmy.dbzer0.com
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        11 months ago

        But mah profits!

        737 Max is still a developing example of what happens when you leave corporate to self-regulate themselves.

      • Starfighter@discuss.tchncs.de
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        11 months ago

        It is, kind of. The plug is secured by 6 stops (or tabs) along each side. The positive pressure differential pushes the plug outwards into those stops.

        To remove the plug you uninstall 4 bolts which allow the plug to go up and over the stops, after which it can hinge outwards on a hinge found at the bottom of the plug.

        Source: https://youtu.be/WhfK9jlZK1o?si=dbUV1i2nNFcNixQh

        • EeeDawg101@lemm.ee
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          11 months ago

          Just seems like a better design would be if no bolts existed (like from them loosening over time and falling off), it would still be sealed perfectly fine. The obvious failure point is the bolts and seems they could do better.

    • GombeenSysadmin
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      11 months ago

      It’s a door plug, which means it’s meant to be replaced with an actual door if required, so a lot of the hardware for an actual door are in place. Doors are designed to slide in, then raise up so the stop pins engage the stop fittings from the inside, so the door is in effect bigger than the hole it’s in. this video provides a detailed explanation of how it works.

      The big issue here is that the airplane is only 2 months old, it was delivered from Boeing in late October. Which means it’s either a design flaw or a process flaw in the original manufacturing. This smacks of corporate cost cutting again. Boeing are totally on the hook for this and it’s only lucky there were no lives lost. You watch, they’ll blame it on the airline initially but the fault will come back round to them again.

    • cobra89@beehaw.org
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      11 months ago

      That’s how the normal doors work because they aren’t permanently secured in place. The reason is weight as it pretty much always is in aviation design.

  • OceanSoap@lemmy.ml
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    11 months ago

    Lovely, I’m flying united to Ireland in two months. Fingers crossed I get an older version.

    • wewbull
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      11 months ago

      Better you’re on the airline where they found the problems than the airline that didn’t.

    • XTornado@lemmy.ml
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      11 months ago

      Ah, playin’ it safe, are ya? Why not spice things up a bit? Flyin’ United, might as well throw in a bit of turbulence for the craic!

  • AutoTL;DR@lemmings.worldB
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    11 months ago

    This is the best summary I could come up with:


    Bolts in need of “additional tightening” have been found during inspections of Boeing 737 Max 9s, United Airlines has said.

    Inspections began after a section of the fuselage fell from an Alaska Airlines 737 Max 9 on Friday.

    United Airlines said “installation issues” relating to door plugs would be “remedied” before the aircraft type would return to service.

    In its statement, United said: “Since we began preliminary inspections on Saturday, we have found instances that appear to relate to installation issues in the door plug - for example, bolts that needed additional tightening.”

    The door plug is a piece of fuselage with a window that can be used as an emergency exit in certain configurations.

    It was this part of the Alaska Airlines plane which dramatically fell off mid-flight over the US state of Oregon, eventually landing in a teacher’s back garden.


    The original article contains 204 words, the summary contains 142 words. Saved 30%. I’m a bot and I’m open source!

  • andmonad@lemmy.world
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    11 months ago

    So are they just going to tighten them up real well and call it a day? Also are these the same planes they were urging the FAA to let them flight without further inspection?

  • Aurix@lemmy.world
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    11 months ago

    I am glad to read all these reports, investigations and of course the emotional laden criticisms of actors associated with this. Because each time I check aviation incidents in Russia, they determine in the first 24 hours it must have been the pilots fault.